2003 GW 330 Express.
Fresh water pump seems to only pressurize when the tank is completely full. I've filled it to overflow 3x today alone and have only used a little water for the head and to wash some dishes (Gauge shows no less than 3/4 full after a little use). I haven't dug around the bilge yet (my least favorite job) but have searched for air leaks around the pump/accumulator (all dry), head and sinks - no signs of problems.
Strange that it works fine when full, but won't pressurize (pump turns off) when I've consumed a little water.
I'll check the filters on the pumps tomorrow but I routinely add a little chlorine to my tank - not sure why clogged filters would work with a full tank but not less than full - and am out of ideas.
FYI, had a lack of pressure problem before, but it was consistent. Found a pinhole leak in the supply line to the head going through the aft bunk forward bilge. Original hose was tight against rough fiberglass (a real disappointment for a Grady).
Don't know if this is somehow related, but it also seems that the head will only pressurize when the fresh water does....Can't tell for sure and now that I've thought about it, can track over the next few days.
Any ideas about where to start?
Fresh water pump seems to only pressurize when the tank is completely full. I've filled it to overflow 3x today alone and have only used a little water for the head and to wash some dishes (Gauge shows no less than 3/4 full after a little use). I haven't dug around the bilge yet (my least favorite job) but have searched for air leaks around the pump/accumulator (all dry), head and sinks - no signs of problems.
Strange that it works fine when full, but won't pressurize (pump turns off) when I've consumed a little water.
I'll check the filters on the pumps tomorrow but I routinely add a little chlorine to my tank - not sure why clogged filters would work with a full tank but not less than full - and am out of ideas.
FYI, had a lack of pressure problem before, but it was consistent. Found a pinhole leak in the supply line to the head going through the aft bunk forward bilge. Original hose was tight against rough fiberglass (a real disappointment for a Grady).
Don't know if this is somehow related, but it also seems that the head will only pressurize when the fresh water does....Can't tell for sure and now that I've thought about it, can track over the next few days.
Any ideas about where to start?
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