- Joined
- Oct 4, 2009
- Messages
- 252
- Reaction score
- 1
- Points
- 16
- Location
- Pass Christian, MS / Baton Rouge, LA
Some of you might have read about the problems I have been having with the electrical system on my 283 Release that is posted on the "Tips, Modifications and Electronics" forum. It seems that I am getting a back-feed of electricity into my switch panel through the aft bilge pump.
Yesterday, Eddie Rowe(SP?) with Grady White called me to thank me for filling out a "satisfaction Survey" a couple of months ago that I had forgotten I had filled out. In our conversation, I mentioned that I was having a problem with the boat and explained it to him.
Today, as promised, he called me back with their engineer, Todd Leggett(SP?) who explained everything to do to fix the problem. Evidently this has happened before and Todd knew exactly what to look for.
For those interested, Seasick hit the nail on the head when he told me that it was a stuck float switch. Good Job!!!
How many manufacturers would send out "satisfaction Surveys", personally call everyone that responded, and then spend the time to call back to help with a problem like this? Maybe others would, but I'll never know. Not likely I'll own anything but a Grady.
BTW, this engineer also discussed the idea I had of installing a diode in the circuit to eliminate the possibility of back feed. He told me where to get it and to be sure it was rated for the proper voltages and amps. He was very knowledgeable.
Hmmm! Maybe this should be a standard item installed at the factory.
Anyway, the only bad news is that I probably will have a new bilge pump on my American Express bill next month.
Thanks to Eddie and Todd (and Seasick) for helping and saving me a lot of time.
Yesterday, Eddie Rowe(SP?) with Grady White called me to thank me for filling out a "satisfaction Survey" a couple of months ago that I had forgotten I had filled out. In our conversation, I mentioned that I was having a problem with the boat and explained it to him.
Today, as promised, he called me back with their engineer, Todd Leggett(SP?) who explained everything to do to fix the problem. Evidently this has happened before and Todd knew exactly what to look for.
For those interested, Seasick hit the nail on the head when he told me that it was a stuck float switch. Good Job!!!
How many manufacturers would send out "satisfaction Surveys", personally call everyone that responded, and then spend the time to call back to help with a problem like this? Maybe others would, but I'll never know. Not likely I'll own anything but a Grady.
BTW, this engineer also discussed the idea I had of installing a diode in the circuit to eliminate the possibility of back feed. He told me where to get it and to be sure it was rated for the proper voltages and amps. He was very knowledgeable.
Hmmm! Maybe this should be a standard item installed at the factory.
Anyway, the only bad news is that I probably will have a new bilge pump on my American Express bill next month.
Thanks to Eddie and Todd (and Seasick) for helping and saving me a lot of time.