- Joined
- Sep 30, 2012
- Messages
- 334
- Reaction score
- 48
- Points
- 28
- Location
- Massachusetts
- Model
- Express 305
Any HPDI experts here?
I am loosing some top end RPM's on one on my 2003 HPDI 150's, changed props and same issue. Compression was good last fall, I plan on checking again, fingers crossed. All filters have been replaced including the metal can filter after VST and mystery filters. Injectors serviced also. Cannot get past 4400 RPMs without overtiming motor. Linkage is ok and TPS shows proper voltage range on YDS. O2 sensor cleaned. I plan on looking around for a fuel leak on the high pressure steel braided lines where they were off to service mystery filters, YDS shows strong fuel pressure with no dips while running. If supply to the HP pump was an issue would the high pressure in YDS dip or be low also?
Over on THT I was recommended a leak down test. If compression is good I don't understand how this will help, on a 2 stroke it would only test head gasket and rings right? Reeds are isolated at top dead center and no valves like in a 4 stroke. I was going to buy a harbor freight leak down tester unless its not needed with a good compression test.
I was hoping for the neutral switch to be the issue but that seems to test ok on YDS in and out of gear. I was so confident I ordered one, might put it in anyways. Motor starts and idles great, slow to catch up on RPMs to the other motor but will catch up to 4400RPMs. If reeds were an issue wouldn't it idle bad?
Also in YDS I was able to kill the spark on each cylinder. On the effected motor engine pitch changed but nothing crazy, unaffected motor RPMs increased but that motor wasn't fully to temp either. How would I go about testing coils? Maybe 1 is bad under load? Anyway to test for that?
Attached are screenshots of YDS with each motor WOT. I know port motor is low RPMs also but figure that will balance out once the other in figured out.
I am loosing some top end RPM's on one on my 2003 HPDI 150's, changed props and same issue. Compression was good last fall, I plan on checking again, fingers crossed. All filters have been replaced including the metal can filter after VST and mystery filters. Injectors serviced also. Cannot get past 4400 RPMs without overtiming motor. Linkage is ok and TPS shows proper voltage range on YDS. O2 sensor cleaned. I plan on looking around for a fuel leak on the high pressure steel braided lines where they were off to service mystery filters, YDS shows strong fuel pressure with no dips while running. If supply to the HP pump was an issue would the high pressure in YDS dip or be low also?
Over on THT I was recommended a leak down test. If compression is good I don't understand how this will help, on a 2 stroke it would only test head gasket and rings right? Reeds are isolated at top dead center and no valves like in a 4 stroke. I was going to buy a harbor freight leak down tester unless its not needed with a good compression test.
I was hoping for the neutral switch to be the issue but that seems to test ok on YDS in and out of gear. I was so confident I ordered one, might put it in anyways. Motor starts and idles great, slow to catch up on RPMs to the other motor but will catch up to 4400RPMs. If reeds were an issue wouldn't it idle bad?
Also in YDS I was able to kill the spark on each cylinder. On the effected motor engine pitch changed but nothing crazy, unaffected motor RPMs increased but that motor wasn't fully to temp either. How would I go about testing coils? Maybe 1 is bad under load? Anyway to test for that?
Attached are screenshots of YDS with each motor WOT. I know port motor is low RPMs also but figure that will balance out once the other in figured out.