1992 Grady 24 Explorer repowered in 03 with a 225 Yamaha 4 Stroke. Last year had some problems with the motor cutting out - had to pump the primer to get it to re-start and run. Possible leak (air?) in the water separator so I replaced the whole assembly with a SS one (Racor with the sight bowl).
While running the other day it would cut out at idle speed (no wake zones) and at trolling speeds. Same thing, pump the primer and it would start and run for about 10 minutes then cut out. Replaced the water separator filter, lines are clean (I have an in line filter prior to the W/S filter which is also clean) and the gas is about 2 months old. Boat runs great at speed (on plane) all day long. As soon as I throttle down for a no wake or trolling, it cuts out afer about 10 minutes at that speed.
My thoughts are an air leak of some sorts??? The fuel filter on the motor is full when this happens (visible filter - you can see the fuel) and the red ring stays on the bottom which is supposed to indicate no water. The fuel line from the motor is 5-6 years old but the primer ball appears to be original (17 years). Haven't had the time yet to trace the fuel line from the filter to the motor (Grady Drive) but I'm guessing that there is a splice in there somewhere.
Any other ideas or similar problems?? This is getting old!
Chris
While running the other day it would cut out at idle speed (no wake zones) and at trolling speeds. Same thing, pump the primer and it would start and run for about 10 minutes then cut out. Replaced the water separator filter, lines are clean (I have an in line filter prior to the W/S filter which is also clean) and the gas is about 2 months old. Boat runs great at speed (on plane) all day long. As soon as I throttle down for a no wake or trolling, it cuts out afer about 10 minutes at that speed.
My thoughts are an air leak of some sorts??? The fuel filter on the motor is full when this happens (visible filter - you can see the fuel) and the red ring stays on the bottom which is supposed to indicate no water. The fuel line from the motor is 5-6 years old but the primer ball appears to be original (17 years). Haven't had the time yet to trace the fuel line from the filter to the motor (Grady Drive) but I'm guessing that there is a splice in there somewhere.
Any other ideas or similar problems?? This is getting old!
Chris