You may have the same problem that I had
I have a 2005 GW tournament with a F250 Yamaha. Upon launching the boat for the first time this year, I could not get the boat on plane. Initially the boat ran fine slightly above idle at about 1200 rpm’s. When I attempted to bring it up to 3,500 RPM’s it stalled before reaching 2,500. From that point on I could barely keep it at idle, it would just stall. I had to get it towed back to the boat ramp were I loaded it back on the trailer and hauled it to Baert Marine GW/Yamaha dealer in Middleton, MA.
At the dealership I explained what had happened and gave them a detailed list of prior work that I had done for winterizing and spring commissioning that could be related to this problem. Specifically, I replaced the 10 micron boat fuel filter and water separator filter on the motor in the fall. I replaced the “F” filter and the VST filter and changed plugs this spring. The tech typed all this information correctly into the repair order (so I thought).
They then hooked it up to a computer and tested fuel pumps and they both worked, but had no fuel pressure, no fuel flow to the motor from the water sep filter. They proceeded to change all the brand new filters that I just put in. (this information never got typed into the repair order) they also changed the plugs which had 10 minutes running time on them. (This was a mix up because the repair order said “replace plugs” instead of “replaced plugs”).
Then they discovered the real problem. The outside of the fuel line at the rigging tube connection to the engine was deteriorated and the fuel line was kinked restricting the flow of fuel. The inside of the coextruded tubing was in good shape but the outer layer was corroded from the leaking E-10 fuel. In addition to the damage to the fuel line the leak also caused the outer jacket of the “Speedo hose” (Throttle cable?) to deteriorate and it needed to be replaced. See pictures. (could not attach?)
The dealer commented that they have seen this before. They also said that a design change was made to fix this problem. They now use Oetiker clamps instead of worm type clamps; also the rigging grommet design has been changed to allow the connection to float freely in the rigging tube. $700. later, Hopefully this has fixed the problem.